OK, this will be more of a 'how to' post than a progress report although it is both. If you have a Shock-Ease fork this may be of interest to you.
First locate part #20 in the patent drawing to see the rubber bushing.
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After looking at the drawing it appears that the bushing is a basic cylinder shape or 'thick washer'. So today I visited my favorite auto parts store with fork in hand to see what I could find.
SIDE NOTE:
I have to point out that this parts store is locally owned and operated by an almost 80 year old man who spent his early years heavily involved with the local drag racing scene. I always patronize his store when I can without regard for 'a better price' at any of the chain stores. You simply cannot replace his years of knowledge. I get frustrated by unqualified counter jockeys at chain stores asking irrelevant questions like "what color is the interior?" when all I want is a distributer cap for my truck (but I digress). I hope that some of you are as lucky as I am to still have an actual owner operated Auto Parts Store or any local service store to visit. Like the old time bike shops, they are a dying breed.
Anyway, After I had asked to see a rubber freeze plug Hugh (the owner) was able to match up in his mind that an engine mount bushing for a 1955 through 1957 Chevy looked like a possible fit. The freeze plug did look just right except for the thickness, but after he walked to the shelf in the back and reemerged with the GM bushing in hand (that also looked like a good fit but for half the price), I handed over the three dollars and change and was on my way!
The only issue was with the thickness of the bushing. I'm sure that somewhere in the world there is a perfect fit sitting on a shelf but for now this would do. Hugh suggested splitting it in half with a band saw and steel mesh gloves but my own wheels began to turn and this is how I approached it:
I first stacked some washers in the space for the bushing on the fork to gauge how thick the bushing should be. Then I marked it on the bushing and pushed a carriage bolt through the center. The square part of the bolt was larger than the hole which gripped the rubber when it was forced in. I then chucked the bolt in my drill press.
Next I took a hack-saw blade and taped it down to two blocks of wood to make it level and placed the blocks on the drill table. The table was then cranked up to the point where the saw blade lined up with the cut line marks.
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Stopping several times to add oil to the blade, I slowly pushed the blade against the bushing as it was spinning in the drill press. When it hit the bolt I stopped and ended up with the desired thickness!
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When I got the fork, someone in the past had stuck an undersized rubber bushing along with a steel washer on each side to replace the original. It probably worked enough to get by at the time, but years later it too crushed and split becoming useless. Here is what I found compared to the newly modified Chevy bushing.
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And finally here is the '55 Chevy bushing on the '37 Shelby fork!
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If it turns out to be too thin after the weight of the bike is on it, I still have the thicker half left over that I can use to further dial in the correct size later on down the road. I hope this helps someone else looking to replace their Shock-Ease bushing.